Thanks guys, and Sandy

give us a break!!
Anyway, where was I.....
So, with the timing checked, all sensors attached, super unleaded topped up, we were ready to check the temporary induction set-up, hoping the even-more-temporary valley gasket would hold out for at least one decent pull. We added another rocker cover gasket to each side to raise the covers above the thicker flanges on the Indy inlet. So the extra worry of oil leaks added to the (mine, at least) tension!
Bearing in mind the engine hadnt seen more than about 3000 revs up to now, Kenny limited the 1st run to 4900 rpm. Timing was kept at a conservative 32deg and no tinkering had been done to the Holley. Ken just knew it would work well enough to check the problem we were having.
Well, as you might imagine, the carb, inlet & Bodgit & Scarper valley pan cover, performed admirably and let the engine pull nicely up to the imposed rev limit.
What's that? You want numbers?
Test 1 - 423hp @ 4900rpm, 455lb-ft @ 4400
With no drama on that pull, we went for another tentative 100rpm and saw
Test 2 - 431hp @ 5000rpm, 459lb-ft @ 4600
So went hell for leather on the 3rd and final run of the day, and stuck it on 5500
Test 3 - 450 @ 5400 (started tailing off at 5500 with 448hp), 457 lb-ft @ 4900
After the 1st test we knew the Carters were causing the problem, so we just did the 2nd & 3rd run because it would be rude not to

We knew not to read too much into the figures with this Holley/Indy set-up, but we were all pretty chuffed with the numbers achieved, considering:
1. the headers on the dyno are over 2" and probably hurting the torque figures and curve - 1-3/4" headers would prob give a better result. Having said that, we're not planning to use headers, but the original cast iron manifolds. Kenny reckons a good set of headers will give you about 70hp over stock cast iron manifolds, but we hope our swoopy max wedge jobbies will be somewhere in between. We'll take them up next time we go to see what difference they do make.
2. Carb & inlet were not adjusted/jetted or matched to the cam/compression etc of the engine as Paul had built it.
3. We stuck to 32deg timimg for this test, so expect to wring a bit out of her with a bit more timing.
4. With the above rectified, using a few more revs might yet see an improvement?
And dont forget this was always intended to be a rebuild to (pretty much) stock specs so as long as we're on the right side of 410hp, we'd be happy
By now it was gone 8.30 and we'd already stopped Kenny from going to a car show in Wakefield (Bill Billadeau had gone there in the ex-Pete W Challenger), so had a quick discussion where to go from here with the rebuild & dyno test, and were away at around 9pm.
As the Carters had already been rebuilt with new gaskets etc before the trip oop to EDA, and we had already tried some adjustments/tuning earlier in the day, all we could think was that some septic (tank, geddit?) over the years before we got the car had been a bit brutal with some d.i.y. tuning an had buggered

some hard-to-see parts like the emulsion tubes.
Without knowledge of any Carter experts that could solve the mystery, we resigned ourselves to the fact that we may need to get a pair of new Edelbrocks that are commonly used as a replacement. Not quite in keeping with our plan of keeping it all as stock as possible, but what can you do ?!
That's how we left it with Kenny & Paul as we departed Friday night. Kenny was going to get in touch with the UK & European Edelbrock rep to see what was available on Sat am.
I spoke to Paul this morning though, and after a night's sleep, had another suggestion for Kenny to try on Monday to see if he can get the poor old Carters' primaries working.
And that's where we are with it at the moment !
Whatever the outcome is, weve got to say a BIG thanks (whether they're looking in or not) to Paul & all at EDA for their help in this. Granted, they're being paid as it's part of their job, but Kenny was more than happy to stay on till we reached a conclusion, and is keen help us to a solution in any way he can.
And Paul was jet-lagged to the gills after coming back from his hols on Tuesday, driving up to Castleford Thurs evening, over to Dave B's Friday evening, then home Friday night.
And thanks again to Dave B.
So a big

to all involved.
Just a shame the Nats is looking doubtful now
